I took it out today and things just got worse until it died. I looked under the tank and the hose that goes from the petcock to carb was off and the gas line had a small crimp. Fixed that and all is welljavascript:emoticon(':motorsmile:')
motorsmile. Full of shits and giggles. I really cant believe how much a difference it made just to adjust the floats and A\F mixture.
"I sure hope those floats are set at 15mm, I don't think there's room in the float bowls to set them to 150mm. Wink
(14.7mm is the recommended setting for most 1G B12's)"
I know, ignorance at it's best. I saw 14.7 and 16 so I shot for in between. I used the cut cardboard method and it worked pretty well.
"I would think the throttle response should be crisp and smooth."
It is now, just that my reassembly wasn't smooth.
"In order to make the 2 inner cylinders run cooler, we run them richer than the outers."
That makes alot of sense but I had drill out the covers so I assume the settings were from factory. The right carb was actually tight and the left was around 4 turns out. You'd think they'd do a little better at the factory. I may have to play around with some fine tuning but it's running well now. Carb sync and a dyno run is on the agenda next.
Sorry about the quotes. I'll have to read the instructions to make them work properly. Thanks.